http://dfwmustangs.net/class/showpro...-oil-pan&cat=9
complete 347 with TFS heads and only a claimed 3000 miles...it's a drag motor but for $3000....buy it!
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http://dfwmustangs.net/class/showpro...-oil-pan&cat=9
complete 347 with TFS heads and only a claimed 3000 miles...it's a drag motor but for $3000....buy it!
Ditto. Really sorry to hear this Marshall. Hope you can source a replacement soon.
Any new theories on what went wrong in the tune?
I'm sorry to hear that too. I'll keep my eyes open for anything that may help you.
What a bummer. Hope everything works out. Let me know if I can help.
I told Richard to get the heads ready. I have my old short block that I might slop together... it's the one that I cracked the water pump mounting ear off the block and JB welded it back together... Would work in a pinch, as long as the JB weld holds.
Kinda frustrating to only have 4 hours on a motor before it goes "pop"...
From the sound of things, your tuner should be paying this bill.
Might consider some sort of air/fuel guage in the future. I would like to have one that records so I could watch a playback to see what it does during a race.
Jerry's issues are also making me think of adding an ATI balancer sooner rather than later.
Talked to the tuner and they are standing behind their tune. If it was safe on the dyno, it should be safe now. Tunes don't change. They insist that something else failed when the cylinders went lean...
I don't know where else to go with this other than patch together a dog to get me through the season (hopefully) and then put the better motor back together next winter for 2013...