Originally Posted by
RichardP
A bit too much on the tune up parts and actually correcting the issue resulted in us diving off the end of the CMC2 chart with three runs at 271. Ooops. I can deal with that though. Some more dyno time and a smaller restrictor should get us back in the box. Thanks to the guys at Houston Performance for squeezing us into their busy dyno schedule (all three times).
I appreciate all the helpful suggestions. A shop that Dan took it to found 7 of the 8 injectors clogged. A fresh set woke it right up. Not sure of the details on what caused that or how to prevent it in the future. The car came with a fuel cell. It has an external fuel pump with a filter before the pump and a filter after the pump. Both filters are these pimpy red anodized jobbers with replaceable elements. I have no clue what is currently in them but my research suggests that the filter before the pump should be a fine stainless steel mesh rated at 100 microns and the filter after the pump should be a paper filter rated at 10 microns. We will make sure they are fresh and proper before we head out. I’m sure we will get some spares while we are at it.
Speaking of spares, does anyone have a set of stock lt1 injectors lying around that we could throw into the trailer in case we haven’t figured out the root cause and need to do another swap at the track?
We head out Monday morning! Hope to see several of you there…
Thanks again,
Richard P.